TY - JOUR
T1 - Numerical analysis and experimental research of shroud casing boundary layer removal on a counter-rotating compressor
AU - Shi, Lei
AU - Liu, Bo
AU - Wu, Xiaoxiong
AU - Na, Zhenzhe
AU - Zhang, Peng
N1 - Publisher Copyright:
©, 2015, AAAS Press of Chinese Society of Aeronautics and Astronautics. All right reserved.
PY - 2015/9/25
Y1 - 2015/9/25
N2 - Domain scaling method is used in the unsteady numerical simulation of a dual-stage axial counter-rotating compressor. Numerical results show that tip leakage vortex over Rotor 2(R2) is the main source of flow blockage in high spanwise and high entropy zone in the tip region, which makes outlet guide vanes in the downstream endure a serious flow condition. Shroud casing boundary layer removal in the high entropy core over rotor tip can make the flow field better and improve the characteristic of compressor. Based on the results of numerical calculation, we redesign and machine the aspirated shroud casing, meanwhile set up boundary layer suction and control system. Experiment is carried out at 1.0% suction rate through R2 tip region shroud casing at 80% corrected rotating speed. Results indicate that boundary layer suction through shroud casing should be used under the massflow with the highest efficiency in original characteristic. Boundary layer suction can better the efficiency and improve the loading level in this flow area. Else it has a negative influence.
AB - Domain scaling method is used in the unsteady numerical simulation of a dual-stage axial counter-rotating compressor. Numerical results show that tip leakage vortex over Rotor 2(R2) is the main source of flow blockage in high spanwise and high entropy zone in the tip region, which makes outlet guide vanes in the downstream endure a serious flow condition. Shroud casing boundary layer removal in the high entropy core over rotor tip can make the flow field better and improve the characteristic of compressor. Based on the results of numerical calculation, we redesign and machine the aspirated shroud casing, meanwhile set up boundary layer suction and control system. Experiment is carried out at 1.0% suction rate through R2 tip region shroud casing at 80% corrected rotating speed. Results indicate that boundary layer suction through shroud casing should be used under the massflow with the highest efficiency in original characteristic. Boundary layer suction can better the efficiency and improve the loading level in this flow area. Else it has a negative influence.
KW - Counter-rotating compressor
KW - Domain scaling method
KW - Operating performance
KW - Shroud casing boundary layer removal
KW - Unsteady calculation
UR - http://www.scopus.com/inward/record.url?scp=84946119384&partnerID=8YFLogxK
U2 - 10.7527/S1000-6893.2014.0340
DO - 10.7527/S1000-6893.2014.0340
M3 - 文章
AN - SCOPUS:84946119384
SN - 1000-6893
VL - 36
SP - 2968
EP - 2980
JO - Hangkong Xuebao/Acta Aeronautica et Astronautica Sinica
JF - Hangkong Xuebao/Acta Aeronautica et Astronautica Sinica
IS - 9
ER -