TY - JOUR
T1 - 突加不平衡下发动机振动响应分析
AU - Zhao, Lu
AU - Liao, Mingfu
AU - Hong, Liang
AU - Lei, Xinliang
AU - Li, Ming
AU - Wang, Siji
AU - Hou, Lizhen
AU - Shao, Zengde
N1 - Publisher Copyright:
© 2022, Editorial Department of Journal of Aerospace Power. All right reserved.
PY - 2022/2
Y1 - 2022/2
N2 - In order to study the sudden unbalance fault of engine, a low⁃pressure rotor model of aero⁃engine was established, and mode check was finished.On this basis, comparison between analysis and test results of the rotor response of test rig under sudden unbalance was conducted.Then analysis model of the rotor⁃support⁃case was established, and comparison between analysis and test results was finished.Result showed that, the angular acceleration term and the transient term of the squeeze film damper, which exist during the actual operation of engine, were taken into account when establishing the rotor⁃support⁃case model, and the analysis results were in agreement with the test results.The relative error between analysis result and test result of vibration displacement response at sudden unbalance position was 2.1%.After checking the responses of the rotor, the support⁃case model was established for response analysis, taking the load of rotor parts as the input of the support⁃case model and considering the characteristics of engine structure.The analysis results were consistent with the test results, with the relative errors between analysis and test results of vibration velocity response near sudden unbalance position no more than 4.7%.The analysis results show the shock characteristics of rotor response after sudden unbalance and the layer attenuation of rotor⁃support⁃case response.The calculation method established has good prospect for promotion.
AB - In order to study the sudden unbalance fault of engine, a low⁃pressure rotor model of aero⁃engine was established, and mode check was finished.On this basis, comparison between analysis and test results of the rotor response of test rig under sudden unbalance was conducted.Then analysis model of the rotor⁃support⁃case was established, and comparison between analysis and test results was finished.Result showed that, the angular acceleration term and the transient term of the squeeze film damper, which exist during the actual operation of engine, were taken into account when establishing the rotor⁃support⁃case model, and the analysis results were in agreement with the test results.The relative error between analysis result and test result of vibration displacement response at sudden unbalance position was 2.1%.After checking the responses of the rotor, the support⁃case model was established for response analysis, taking the load of rotor parts as the input of the support⁃case model and considering the characteristics of engine structure.The analysis results were consistent with the test results, with the relative errors between analysis and test results of vibration velocity response near sudden unbalance position no more than 4.7%.The analysis results show the shock characteristics of rotor response after sudden unbalance and the layer attenuation of rotor⁃support⁃case response.The calculation method established has good prospect for promotion.
KW - Load
KW - Low⁃pressure rotor
KW - Rotor⁃support⁃case system
KW - Sudden unbalance
KW - Transient calculation
UR - http://www.scopus.com/inward/record.url?scp=85126514600&partnerID=8YFLogxK
U2 - 10.13224/j.cnki.jasp.20210014
DO - 10.13224/j.cnki.jasp.20210014
M3 - 文章
AN - SCOPUS:85126514600
SN - 1000-8055
VL - 37
SP - 251
EP - 262
JO - Hangkong Dongli Xuebao/Journal of Aerospace Power
JF - Hangkong Dongli Xuebao/Journal of Aerospace Power
IS - 2
ER -