The analysis on the rising section of experimental pressure in variable thrust pintle solid rocket motor

Xiang Geng Wei, Guo Qiang He, Jiang Li, Zhan Feng Zhou

科研成果: 书/报告/会议事项章节会议稿件同行评审

11 引用 (Scopus)

摘要

The experimental system of non-coaxial pintle solid rocket motor was designed, and through this system, the experiments that validate variable thrust principle were carried out. A series of experiments were done, so as to find out how motor free volume, pintle movement state, cylinder sending pintle to some position by one time or not, equivalent throat structure, and propellant influence the response of pressure during the change of thrust. And by analyzing the results, it is concluded that the response time of propellant is the primary factor which effects the response of pressure.

源语言英语
主期刊名44th AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit
出版状态已出版 - 2008
活动44th AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit - Hartford, CT, 美国
期限: 21 7月 200823 7月 2008

出版系列

姓名44th AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit

会议

会议44th AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit
国家/地区美国
Hartford, CT
时期21/07/0823/07/08

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