TY - JOUR
T1 - Experimental investigation on two-phase pulse detonation engine
AU - Fan, Wei
AU - Yan, Chuanjun
AU - Huang, Xiqiao
AU - Zhang, Qun
AU - Zheng, Longxi
PY - 2003/6/1
Y1 - 2003/6/1
N2 - This paper presents some results of experimental investigation on a two-phase pulse detonation engine (PDE) model. Proof-of-principle experiments of this model with liquid C8H16/air mixture were successfully conducted. Efforts were focused on initiation and propagation of detonation waves by means of one-step detonation initiation method, low-energy ignition system (total stored energy of 50 mJ), and effective Schelkin spiral. Three PDE models with different sizes were tested: 30 mm-I.D. by 2 m-length; 56 mm-I.D. by 2 m-length and 50 mm by 1 m, which were operated over a repetition frequency range from 1 Hz to 36 Hz. One-way valves were used to adaptively control intermittent supplies of air and fuel flows. The results of detonation velocity, over-pressure and impulse measurements were presented. The measured pressure ratio of detonation wave was close to that of C-J detonation. The effects of equivalence ratio, PDE diameter, length, and detonation frequency on its performance were experimentally investigated. The obtained results have demonstrated that the averaged thrust of PDE is approximately proportional to the volume of detonation chamber and detonation frequency. For liquid C8H16/air mixture, the PDE operation with as short a length as 1000 mm and detonation frequency up to 36 Hz was successfully realized, which made an important step to practical PDE.
AB - This paper presents some results of experimental investigation on a two-phase pulse detonation engine (PDE) model. Proof-of-principle experiments of this model with liquid C8H16/air mixture were successfully conducted. Efforts were focused on initiation and propagation of detonation waves by means of one-step detonation initiation method, low-energy ignition system (total stored energy of 50 mJ), and effective Schelkin spiral. Three PDE models with different sizes were tested: 30 mm-I.D. by 2 m-length; 56 mm-I.D. by 2 m-length and 50 mm by 1 m, which were operated over a repetition frequency range from 1 Hz to 36 Hz. One-way valves were used to adaptively control intermittent supplies of air and fuel flows. The results of detonation velocity, over-pressure and impulse measurements were presented. The measured pressure ratio of detonation wave was close to that of C-J detonation. The effects of equivalence ratio, PDE diameter, length, and detonation frequency on its performance were experimentally investigated. The obtained results have demonstrated that the averaged thrust of PDE is approximately proportional to the volume of detonation chamber and detonation frequency. For liquid C8H16/air mixture, the PDE operation with as short a length as 1000 mm and detonation frequency up to 36 Hz was successfully realized, which made an important step to practical PDE.
KW - Experimental investigation
KW - Two-phase pulse detonation engine
UR - http://www.scopus.com/inward/record.url?scp=0038385186&partnerID=8YFLogxK
U2 - 10.1016/S0010-2180(03)00043-9
DO - 10.1016/S0010-2180(03)00043-9
M3 - 文章
AN - SCOPUS:0038385186
SN - 0010-2180
VL - 133
SP - 441
EP - 450
JO - Combustion and Flame
JF - Combustion and Flame
IS - 4
ER -