摘要
Combined with theoretical simulation of the beat vibration, analysis of the measured vibration signal and summary of the actual vibration elimination experience, three multi-source beat vibration modes of aero-engines were discussed. The identification process and the elimination method of the beat vibration fault were established. Experimental verification showed that for the three common multi-source coupling beat modes, the multi-source beat vibration and the vibration fluctuation could be eliminated when the multi-source excitation frequency differed by more than 3%. The proposed process and method were implemented and verified in engine beat vibration and fluctuation trouble-shooting, and the low-pressure rotor 2 times frequency-high-pressure rotor fundamental frequency coupled beat vibration was accurately identified. The low-pressure rotor speed was well-tuned through the control schedule to separate the above two frequencies by 3%. The vibration fluctuations caused by beat vibration was eliminated and the proposed method was validated.
投稿的翻译标题 | Experimental validation of the beat vibration of aero-engine |
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源语言 | 繁体中文 |
页(从-至) | 2639-2647 |
页数 | 9 |
期刊 | Hangkong Dongli Xuebao/Journal of Aerospace Power |
卷 | 38 |
期 | 11 |
DOI | |
出版状态 | 已出版 - 11月 2023 |
关键词
- beat vibration
- excitation frequency
- multi-source excitation
- vibration
- vibration fluctuation