航空发动机拍振问题研究与验证

Xiaofei Ding, Mingfu Liao, Danyang Peng, Fangjun Han

科研成果: 期刊稿件文章同行评审

1 引用 (Scopus)

摘要

Combined with theoretical simulation of the beat vibration, analysis of the measured vibration signal and summary of the actual vibration elimination experience, three multi-source beat vibration modes of aero-engines were discussed. The identification process and the elimination method of the beat vibration fault were established. Experimental verification showed that for the three common multi-source coupling beat modes, the multi-source beat vibration and the vibration fluctuation could be eliminated when the multi-source excitation frequency differed by more than 3%. The proposed process and method were implemented and verified in engine beat vibration and fluctuation trouble-shooting, and the low-pressure rotor 2 times frequency-high-pressure rotor fundamental frequency coupled beat vibration was accurately identified. The low-pressure rotor speed was well-tuned through the control schedule to separate the above two frequencies by 3%. The vibration fluctuations caused by beat vibration was eliminated and the proposed method was validated.

投稿的翻译标题Experimental validation of the beat vibration of aero-engine
源语言繁体中文
页(从-至)2639-2647
页数9
期刊Hangkong Dongli Xuebao/Journal of Aerospace Power
38
11
DOI
出版状态已出版 - 11月 2023

关键词

  • beat vibration
  • excitation frequency
  • multi-source excitation
  • vibration
  • vibration fluctuation

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