TY - JOUR
T1 - Effects of segmented layer suction and micro-vortex generator on a high-load compressor cascade performance
AU - Ma, Shan
AU - Chu, Wuli
AU - Sun, Xiaolin
AU - Guo, Zhengtao
AU - Yan, Song
N1 - Publisher Copyright:
© IMechE 2021.
PY - 2021/11
Y1 - 2021/11
N2 - The axial location of full-span boundary layer suction is studied to explore the influences of suction slot on the cascade performance. At the design condition, the slot with 50% axial location shows a superior capability to reduce the total pressure loss. At the near stall condition, the more upstream of the suction slot is moved, the more total pressure loss is reduced, and the suction slot with a location of 0.7 axial chord length cannot effectively reduces the total pressure loss in all conditions. Moreover, a rearranged segmented suction slot according to the distribution characteristics of the flow reversal region is developed and compared with full-span boundary layer suction. The segmented suction slot shows significant advantages in delaying the stall occurrence, and the stall point is delayed from 7.9° to 10.0° compared with the baseline. According to a quantitative analysis method selected to measure the performances of flow control technologies, the wake loss is significantly reduced by the segmented suction slot. Finally, a set of micro-vortex generator is introduced in the cascade with a segmented suction slot, and the conclusion indicates that the portion near the end-wall is very effective to reduce the flow loss.
AB - The axial location of full-span boundary layer suction is studied to explore the influences of suction slot on the cascade performance. At the design condition, the slot with 50% axial location shows a superior capability to reduce the total pressure loss. At the near stall condition, the more upstream of the suction slot is moved, the more total pressure loss is reduced, and the suction slot with a location of 0.7 axial chord length cannot effectively reduces the total pressure loss in all conditions. Moreover, a rearranged segmented suction slot according to the distribution characteristics of the flow reversal region is developed and compared with full-span boundary layer suction. The segmented suction slot shows significant advantages in delaying the stall occurrence, and the stall point is delayed from 7.9° to 10.0° compared with the baseline. According to a quantitative analysis method selected to measure the performances of flow control technologies, the wake loss is significantly reduced by the segmented suction slot. Finally, a set of micro-vortex generator is introduced in the cascade with a segmented suction slot, and the conclusion indicates that the portion near the end-wall is very effective to reduce the flow loss.
KW - boundary layer suction
KW - Compressor cascade
KW - corner separation
KW - corner stall
KW - micro-vortex generator
UR - http://www.scopus.com/inward/record.url?scp=85099933114&partnerID=8YFLogxK
U2 - 10.1177/0954406220980502
DO - 10.1177/0954406220980502
M3 - 文章
AN - SCOPUS:85099933114
SN - 0954-4062
VL - 235
SP - 5309
EP - 5323
JO - Proceedings of the Institution of Mechanical Engineers, Part C: Journal of Mechanical Engineering Science
JF - Proceedings of the Institution of Mechanical Engineers, Part C: Journal of Mechanical Engineering Science
IS - 21
ER -